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US Airways 1549 NTSB Sunshine Meeting

US Airways 1549 NTSB Sunshine MeetingFor those of you interested in the NTSB background for the movie Sully https://www.sully-movie.com

Courtesy: NTSB – Aircraft Accident Report – Loss of Thrust in Both Engines After Encountering a Flock of Birds and Subsequent Ditching on the Hudson River, US Airways Flight 1549, Airbus A320-214, N106US, Weehawken, New Jersey, January 15, 2009.

A synopsis of the Board’s report, including the probable cause, conclusions, and recommendations, is available on the NTSB’s website, athttps://www.ntsb.gov/investigations/Ac…

Washington, DC – In addition to the decisions and actions of the flight crewmembers, overwater safety equipment likely saved lives that might have otherwise been lost to drowning, the NTSB said.

The Safety Board met to conclude its 15-month investigation into the January 15, 2009, accident in which a US Airways A320 jetliner bound for Charlotte was ditched into the Hudson River after striking a flock of Canada geese shortly after departing New Yorks LaGuardia Airport. All of the 150 passengers and five crewmembers survived.

Investigators said that had the airplane not been equipped with forward slide/rafts, many of the 64 occupants of those rafts would likely have been submerged in the 41-degree Hudson River, potentially causing a phenomenon called cold shock, which can lead to drowning in as little as five minutes.

The accident flight had the additional safety equipment available only because the particular aircraft operated that day happened to be certified for extended overwater (EOW) operations even though current FAA regulations did not require the flight from New York to Charlotte to be so equipped.

Good visibility, calm waters, and proximity of passenger ferries, which rescued everyone on flight 1549 within 20 minutes, were other post-accident factors the Safety Board credited with the survival of all aboard the aircraft.

Once the birds and the airplane collided and the accident became inevitable, so many things went right, said NTSB Chairman Deborah A.P. Hersman. This is a great example of the professionalism of the crewmembers, air traffic controllers and emergency responders who all played a role in preserving the safety of everyone aboard.

The Safety Board said that the probable cause of the accident was the ingestion of large birds into each engine, resulting in an almost total loss of engine power. Contributing to the severity of the fuselage damage and resulting unavailability of the aft slide/rafts, the Board cited the FAAs inadequate ditching certification standards, lack of industry training on ditching techniques, and the captains resulting difficulty maintaining his intended airspeed on final approach due to task saturation resulting from the emergency situation.

The report adopted by the Safety Board today validated the Captains decision to ditch into the Hudson River saying that it provided the highest probability that the accident would be survivable. Contributing to the survivability of the accident was the crew resource management between the captain and first officer, which allowed them to maintain control of the airplane, increasing the survivability of the impact with the water.

In addressing the hazards that birds pose to aircraft of all sizes, the report noted that most bird strike events occur within 500 feet of the ground while flight 1549 struck geese at 2700 feet. Investigators said that this difference demonstrates that bird strike hazards to commercial aircraft are not limited to any predictable scenario.

Concluding that engine screens or changes to design would not be a viable solution to protect against bird ingestion events on commercial jetliners, the Board made it clear that the potential for significant damage from encounters with birds remains a challenge to the aviation community.

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